Done
Posted: Mon Sep 27, 2004 5:18 am
I finally got around to doing the job. I tore everything down and replaced the oil pump, oil pump O-ring, water pump, water pump gasket, thermostat, thermostat gasket, crank seal, all cam seals, timing belt, drive belts, upper & lower radiator hoses, oil, oil filter and coolant. I think that's it. Oh yeah, and I swapped a little blood with oil, but not as much as usual. You'll have that.
So how did it go with the DOHC? Well, not TOO bad. I'll try to keep it as short and informative as possible.
Removing the radiator w/fans, drive belts, tensioners, belt covers, etc., off the front was much easier than the gen 1. The front of the motor is angled upwards and there is more room to work than there is with the gen 1. The alternator, A/C compressor and all related drive belts and tensioners are all pretty much identical to the gen 1 components. The timing belt cover is also a much better design than the gen 1. It easily dissembles without breaking bolts, etc. The rubber seals on the center cover still get impregnated with oil and contaminates and swell up complicating reinstallation though. Not too big of a deal.
The camshaft sprockets: PITA.
Seeing in the manual that these sprockets had a hex head on each one, I was thinking that it should be easy to hold them in place while I broke loose and torqued the sprocket bolts back down. Wrong. With the MT in first gear, I broke each bolt loose, but it was kind of nerve-racking since the crank still moved a lot even then. Still, I got them loose. Reassembly was another issue.
Although I have never replaced a gen 1 oil pump, the gen 2 oil pump also appeared identical to the gen 1. As for the water pump, I think it’s identical to the gen 1. If you cross-reference both of the parts, I bet they’re the same, just as the installation. Installation of them was a bit of a pain, just because you have to try to line everything up from the crank angle to the oil pump to the fastening bolts and seals while trying to keep the rubber O-ring in place and the bead of sealant on the oil pump (I used the recommended Permatex Ultra-gray). I got the oil pump almost in place and had to pull it back off three times for various reasons, including the new crank seal folding outwards instead of sliding into place once. That sucked. The oil pump was a PITA. I was getting tired at that point though. The water pump wasn’t too bad. The metal gasket was bent, warped and uncooperative as usual, which was aggravating, but not too bad. The crank seal was easy since I replaced the oil pump, which is where it’s seated. The cam seals weren’t too bad. Breaking the cam sprocket bolts loose wasn’t too bad since I did it while the old T-belt was still installed and the car was in gear. I then used and broke my ultimate best various-use tool ever (a bent screwdriver that I made when I was 14) to pull the two right seals, in which it was doing a killer job (email me or post here and I’ll explain) so for the other two cam seals, I went back to using my old method of carefully drilling a single small hole in each seal with my dremel tool and carefully screwing a drywall screw into the hole until it got a firm grip, then prying it out by using a needle-nose plyer to grip the head of the screw and carefully leveraging it against the camshaft, while, when necessary, placing another small screwdriver between the screw and the camshaft in order to keep the two from touching and scoring. To replace and seat the new seals, I used the old big socket and mallet method to seat them firmly in place, oiling everything up first, of course. That’s the easy part.
The next step was to replace the cam sprockets. No big deal, but also no way to torque them down, so as planned, I waited until the belt was in place. I tried to snug them up a little anyway and the exhaust cam on the left side spun under pressure since it was, well under pressure. I just grabbed it with my channel locks and rotated it (counter-clockwise, which is the only way you want to spin that one) back to its happy place and it sat there again by itself. Apparently it was balancing on the top of its cam lobe. That was the end of day one.
The following day, I cleaned up the idler pulleys, tensioners, etc., while powering down my caffeine and rubbing out the eye boogers. I then followed the directions, installed the necessary idlers, compressed and installed the tensioner and prepped everything for the timing belt, then ate an eggy sandwich while I looked everything over.
I put the belt on in the order recommended for the DOHC motor. All went well. Too well. Made me nervous. Got the belt in place. Checked the timing belt marks, and then pulled the pin on the tensioner. Smiled. Thought all was good. Since I then had the belt in place and under tension, I decided to rely on the belt to hold the cams in place while I torqued down the sprocket bolts since it worked the other way. Note: DON’T DO THAT. When I thought my torque wrench was signaling that it was hitting 55 ft-lbs, it was actually the belt jumping a tooth on the crank sprocket. DOH! In hindsight, it made sense since, by cranking the right intake cam sprocket, I was relieving belt tension at the next sprocket, which was the crank. Everything else was still in check. I considered taking up smoking again and/or placing my head in my vice for being such a damn fool.
Fortunately, my plan to VERY CAREFULLY pull the idler pulley to the left crank sprocket and VERY CAREFULLY rotate the crank back a couple degrees via my torque wrench and put everything back in place worked. Whew.
I have been drinking a lot at this point. Not while doing the work, but now while writing this and celebrating the fact that I’m done working on this god-forsaken car. So… thanks for reading this far. I’m just trying to help the next poor sap that has to go through this <g> actually, it’s really not so bad. I just like to bitch. Read on…
At this point, the belt was on and I double and triple-checked the marks on the belts, sprockets, etc., and it was all good. Yay me.
Now for the ugly part. I had to get 55-61 ft-lbs of torque on each of the four cam sprocket bolts. That was a major pain in the ass. Since I managed the make the belt jump a tooth on the first attempt, I realized that relying on the belt was incredibly stupid. My bad. SO.. back to the channel locks on crappy plastc sprocket hex heads. Yes, plastic. Getting my channel locks on the right side and trying to hold that while I powered down the torque wrench with the other side wasn’t easy, obviously. I finally got them both after about a half hour of shouting profanities and throwing tools across the street (then going to find them)
The other side was twice as bad.
This side, the hex head was deeper inside the sprocket. The best I could do with my channel locks was probably about a total of 8mm surface coverage and the best death grip I could do after two days of working on this thing. It took another hour and I actually considered giving up at 40lbs of torque (instead of 55) because I couldn’t get any further. Did I mention that these sprockets are PLASTIC???? Junk. Well, I persisted and got them all to 55-58 ft lbs.
It was all down hill from there.
The rest was your usual reassembly. No big deal. Had to put the T-belt covers back on, main pulley, drive belts, radiator and fans, hoses, etc. Pretty easy.
Drove it for a while and it seems to be fine. Doesn’t seem to be leaking any oil. Happy car. Should be good for quite a while now.
To summarize, it was a lot more work, a LOT more stress and, while I would do it again if I had to, I would rather not. The SOHC design is much easier. I could do that in my sleep now. I think I did my SOHC 2.2T in 6-8 hours, this one probably took me twice as long, but this is the first time I did the oil pump. I take my time and clean the sh*t out of everything, etc., so that’s why it seems excessive. That’s also why I do everything myself.
All is good now.
Thanks to everyone for their input in this. I hope this helps anything that plans to do this themselves. Email me and I’ll be happy to help.
Thanks,
Dave
So how did it go with the DOHC? Well, not TOO bad. I'll try to keep it as short and informative as possible.
Removing the radiator w/fans, drive belts, tensioners, belt covers, etc., off the front was much easier than the gen 1. The front of the motor is angled upwards and there is more room to work than there is with the gen 1. The alternator, A/C compressor and all related drive belts and tensioners are all pretty much identical to the gen 1 components. The timing belt cover is also a much better design than the gen 1. It easily dissembles without breaking bolts, etc. The rubber seals on the center cover still get impregnated with oil and contaminates and swell up complicating reinstallation though. Not too big of a deal.
The camshaft sprockets: PITA.
Seeing in the manual that these sprockets had a hex head on each one, I was thinking that it should be easy to hold them in place while I broke loose and torqued the sprocket bolts back down. Wrong. With the MT in first gear, I broke each bolt loose, but it was kind of nerve-racking since the crank still moved a lot even then. Still, I got them loose. Reassembly was another issue.
Although I have never replaced a gen 1 oil pump, the gen 2 oil pump also appeared identical to the gen 1. As for the water pump, I think it’s identical to the gen 1. If you cross-reference both of the parts, I bet they’re the same, just as the installation. Installation of them was a bit of a pain, just because you have to try to line everything up from the crank angle to the oil pump to the fastening bolts and seals while trying to keep the rubber O-ring in place and the bead of sealant on the oil pump (I used the recommended Permatex Ultra-gray). I got the oil pump almost in place and had to pull it back off three times for various reasons, including the new crank seal folding outwards instead of sliding into place once. That sucked. The oil pump was a PITA. I was getting tired at that point though. The water pump wasn’t too bad. The metal gasket was bent, warped and uncooperative as usual, which was aggravating, but not too bad. The crank seal was easy since I replaced the oil pump, which is where it’s seated. The cam seals weren’t too bad. Breaking the cam sprocket bolts loose wasn’t too bad since I did it while the old T-belt was still installed and the car was in gear. I then used and broke my ultimate best various-use tool ever (a bent screwdriver that I made when I was 14) to pull the two right seals, in which it was doing a killer job (email me or post here and I’ll explain) so for the other two cam seals, I went back to using my old method of carefully drilling a single small hole in each seal with my dremel tool and carefully screwing a drywall screw into the hole until it got a firm grip, then prying it out by using a needle-nose plyer to grip the head of the screw and carefully leveraging it against the camshaft, while, when necessary, placing another small screwdriver between the screw and the camshaft in order to keep the two from touching and scoring. To replace and seat the new seals, I used the old big socket and mallet method to seat them firmly in place, oiling everything up first, of course. That’s the easy part.
The next step was to replace the cam sprockets. No big deal, but also no way to torque them down, so as planned, I waited until the belt was in place. I tried to snug them up a little anyway and the exhaust cam on the left side spun under pressure since it was, well under pressure. I just grabbed it with my channel locks and rotated it (counter-clockwise, which is the only way you want to spin that one) back to its happy place and it sat there again by itself. Apparently it was balancing on the top of its cam lobe. That was the end of day one.
The following day, I cleaned up the idler pulleys, tensioners, etc., while powering down my caffeine and rubbing out the eye boogers. I then followed the directions, installed the necessary idlers, compressed and installed the tensioner and prepped everything for the timing belt, then ate an eggy sandwich while I looked everything over.
I put the belt on in the order recommended for the DOHC motor. All went well. Too well. Made me nervous. Got the belt in place. Checked the timing belt marks, and then pulled the pin on the tensioner. Smiled. Thought all was good. Since I then had the belt in place and under tension, I decided to rely on the belt to hold the cams in place while I torqued down the sprocket bolts since it worked the other way. Note: DON’T DO THAT. When I thought my torque wrench was signaling that it was hitting 55 ft-lbs, it was actually the belt jumping a tooth on the crank sprocket. DOH! In hindsight, it made sense since, by cranking the right intake cam sprocket, I was relieving belt tension at the next sprocket, which was the crank. Everything else was still in check. I considered taking up smoking again and/or placing my head in my vice for being such a damn fool.
Fortunately, my plan to VERY CAREFULLY pull the idler pulley to the left crank sprocket and VERY CAREFULLY rotate the crank back a couple degrees via my torque wrench and put everything back in place worked. Whew.
I have been drinking a lot at this point. Not while doing the work, but now while writing this and celebrating the fact that I’m done working on this god-forsaken car. So… thanks for reading this far. I’m just trying to help the next poor sap that has to go through this <g> actually, it’s really not so bad. I just like to bitch. Read on…
At this point, the belt was on and I double and triple-checked the marks on the belts, sprockets, etc., and it was all good. Yay me.
Now for the ugly part. I had to get 55-61 ft-lbs of torque on each of the four cam sprocket bolts. That was a major pain in the ass. Since I managed the make the belt jump a tooth on the first attempt, I realized that relying on the belt was incredibly stupid. My bad. SO.. back to the channel locks on crappy plastc sprocket hex heads. Yes, plastic. Getting my channel locks on the right side and trying to hold that while I powered down the torque wrench with the other side wasn’t easy, obviously. I finally got them both after about a half hour of shouting profanities and throwing tools across the street (then going to find them)
The other side was twice as bad.
This side, the hex head was deeper inside the sprocket. The best I could do with my channel locks was probably about a total of 8mm surface coverage and the best death grip I could do after two days of working on this thing. It took another hour and I actually considered giving up at 40lbs of torque (instead of 55) because I couldn’t get any further. Did I mention that these sprockets are PLASTIC???? Junk. Well, I persisted and got them all to 55-58 ft lbs.
It was all down hill from there.
The rest was your usual reassembly. No big deal. Had to put the T-belt covers back on, main pulley, drive belts, radiator and fans, hoses, etc. Pretty easy.
Drove it for a while and it seems to be fine. Doesn’t seem to be leaking any oil. Happy car. Should be good for quite a while now.
To summarize, it was a lot more work, a LOT more stress and, while I would do it again if I had to, I would rather not. The SOHC design is much easier. I could do that in my sleep now. I think I did my SOHC 2.2T in 6-8 hours, this one probably took me twice as long, but this is the first time I did the oil pump. I take my time and clean the sh*t out of everything, etc., so that’s why it seems excessive. That’s also why I do everything myself.
All is good now.
Thanks to everyone for their input in this. I hope this helps anything that plans to do this themselves. Email me and I’ll be happy to help.
Thanks,
Dave