DAMN RATTLE I HAVE CONQUERED YOU!!
Posted: Tue Sep 21, 2004 4:06 am
I found that damn rattle tonight that's been driving me nuts since the swap. I took apart the dash again, and it just seemed like it was up in the dash....but there's no metal up there. I pulled into the garage several times, and could hear it from outside.
I had a friend come over, and stick his head under the engine bay while I let off on the clutch a little with the brake on....yeah I know....reall good for the clutch. He said it's either below the ignitor, or behind the firewall. I take a gander and start feeling things......low and behold my dumb crack ass forgot to tighten the bolt that holds the pitch stop mount to the chassis!!! I must have loosened it enough so it would move, but never tightened it back up.
So I tightened the little whore up, and BAM, no more rattle!!!!
I now have to put my dash back together again. The one weird thing though is that my gas gauge went all the way to E randomly.....I wiggled the gauge cluster, and it came back up to 1/4 tank. I thought I had a little more then that, but I might be mistaken. Hopefully none of the wires got loose or messed up when moving the cluster around.
And I got the clutch adjusted so it doesn't rattle and there's still a little play......so the two main issues I had are taken care of.
Ok....I'm done rambling
I had a friend come over, and stick his head under the engine bay while I let off on the clutch a little with the brake on....yeah I know....reall good for the clutch. He said it's either below the ignitor, or behind the firewall. I take a gander and start feeling things......low and behold my dumb crack ass forgot to tighten the bolt that holds the pitch stop mount to the chassis!!! I must have loosened it enough so it would move, but never tightened it back up.
So I tightened the little whore up, and BAM, no more rattle!!!!
I now have to put my dash back together again. The one weird thing though is that my gas gauge went all the way to E randomly.....I wiggled the gauge cluster, and it came back up to 1/4 tank. I thought I had a little more then that, but I might be mistaken. Hopefully none of the wires got loose or messed up when moving the cluster around.
And I got the clutch adjusted so it doesn't rattle and there's still a little play......so the two main issues I had are taken care of.
Ok....I'm done rambling
