One hell of a weekend installing the WRX TMIC
Posted: Tue Aug 30, 2005 9:23 am
SO its in.
I started on Friday after my classes after having the ic adorn my room for about 3 weeks. The first day not so bad pulled the intake box, all the essential hoses and fittings, did some minor pounding and a few test fits to see what else was keeping me from fitting the thing in there. The AC line was a differnet story however BUT what actually seems to be working really well is i rerouted it under the dog bone (stablization piece from engine to firewall) and it pulled it down enough outa the way that the IC still hit the top of the hood but just barely. (by the way I own a 93 wagon so i have a 4EAT) but by this time it was bout 630 and the bugs at my friends house were horrible so i called it a day.
Day two..... after a slow start (recovering from the night before) at 230 got the adapter plate (the one from the hardware store parts that Vrg3 suggested) all JBwelded up and reran new coolent lines and then the bbq started and didnt end till i couldnt see strait (got to love college).
Day three was the kicker. I got the thing to fit in nicely and after 3 trips to the autostore and a tour of the back room of NAPA resulted in having it all plumbed and kink free and i mean not a kink anywhere ( which was the happiest moment of the whole project). but the buggs got even worse from the other night and i had lost the two bolts to mount the bov adapter plate and stared dropping things through the engine bay so unhappily i called it a night.
So after a long day of classes today i finally got the DV plumbed, all the hoses reran, MBC put in, everything put back together and then decided i didnt like the DV plumbing so i took it out only to drop it and break off the nipple on the top..... SO it was back to the store for some superglue and about 2 hours later she was running and i cant tell you how much i loved that "I just finished victory beer."
* Pics soon*
There is one thing that concerns me however:
Before the ic i had the Coffee cup mod, and had taken out the snorkel. And with this set up when ever i was just getting outa boost and entering vaccum (2000-2500 rpms) i would hear a low growl coming from what sounded like my air box. Is this normal? because now when it approches this range or only sometimes when it "blows off" it make this sorta Farting / thump sound and i didnt mind the growl before but now its just horrible sounding and i dont know if maybe its because of the longer DV plumbing or if there is a diaphram in the DV that migh have busted pre or post drop? but it needs to be fixed cause its almost approching "ridiculous sounding"
I started on Friday after my classes after having the ic adorn my room for about 3 weeks. The first day not so bad pulled the intake box, all the essential hoses and fittings, did some minor pounding and a few test fits to see what else was keeping me from fitting the thing in there. The AC line was a differnet story however BUT what actually seems to be working really well is i rerouted it under the dog bone (stablization piece from engine to firewall) and it pulled it down enough outa the way that the IC still hit the top of the hood but just barely. (by the way I own a 93 wagon so i have a 4EAT) but by this time it was bout 630 and the bugs at my friends house were horrible so i called it a day.
Day two..... after a slow start (recovering from the night before) at 230 got the adapter plate (the one from the hardware store parts that Vrg3 suggested) all JBwelded up and reran new coolent lines and then the bbq started and didnt end till i couldnt see strait (got to love college).
Day three was the kicker. I got the thing to fit in nicely and after 3 trips to the autostore and a tour of the back room of NAPA resulted in having it all plumbed and kink free and i mean not a kink anywhere ( which was the happiest moment of the whole project). but the buggs got even worse from the other night and i had lost the two bolts to mount the bov adapter plate and stared dropping things through the engine bay so unhappily i called it a night.
So after a long day of classes today i finally got the DV plumbed, all the hoses reran, MBC put in, everything put back together and then decided i didnt like the DV plumbing so i took it out only to drop it and break off the nipple on the top..... SO it was back to the store for some superglue and about 2 hours later she was running and i cant tell you how much i loved that "I just finished victory beer."
* Pics soon*
There is one thing that concerns me however:
Before the ic i had the Coffee cup mod, and had taken out the snorkel. And with this set up when ever i was just getting outa boost and entering vaccum (2000-2500 rpms) i would hear a low growl coming from what sounded like my air box. Is this normal? because now when it approches this range or only sometimes when it "blows off" it make this sorta Farting / thump sound and i didnt mind the growl before but now its just horrible sounding and i dont know if maybe its because of the longer DV plumbing or if there is a diaphram in the DV that migh have busted pre or post drop? but it needs to be fixed cause its almost approching "ridiculous sounding"