Stalling after MBC
Posted: Sat Jan 13, 2007 2:40 am
I think I have an idea of why Im having a problem, I just wanted to double check with you guys. Im still learning about turbos, so this is a learning experience for me.
I built a MBC yesterday. I want to buy a Hallman, but I figured a DIY one would be good for 10-12 PSI until I get an intercooler.
I installed it tonight using the directions from the write up in the library. I took it out and when I left my driveway it made 10psi of boost. I was only on it for a second to see how much boost it was making. I made it about 1/8th of a mile down the street, and going up a hill, just as it was about to make boost, the check engine light came on and it stalled. It wouldnt start back up again, so I rolled down the hill in neutral, and it started right up. I went home, double check all my connections, and went back out. Leaving the driveway it made 10psi fine. I got a couple hundred feet and the CEL came back on. Going up the hill it almost stalled, but I was able to save it. I made it to the end of the street and turned around. I gave it soem gas to see if it would make boost, and just as it was about to, it stalled again.
Now, heres what I think is the problem. I already had a T fitting on the vaccum line after the purge valve I was using for my boost gauge, so I used that for the MBC. Would this cause the CEL and the stalling? Im friggin freezing, so tomorrow Im going to move the T to before the purge valve and see if that makes a difference.
Thanks for any help.
I built a MBC yesterday. I want to buy a Hallman, but I figured a DIY one would be good for 10-12 PSI until I get an intercooler.
I installed it tonight using the directions from the write up in the library. I took it out and when I left my driveway it made 10psi of boost. I was only on it for a second to see how much boost it was making. I made it about 1/8th of a mile down the street, and going up a hill, just as it was about to make boost, the check engine light came on and it stalled. It wouldnt start back up again, so I rolled down the hill in neutral, and it started right up. I went home, double check all my connections, and went back out. Leaving the driveway it made 10psi fine. I got a couple hundred feet and the CEL came back on. Going up the hill it almost stalled, but I was able to save it. I made it to the end of the street and turned around. I gave it soem gas to see if it would make boost, and just as it was about to, it stalled again.
Now, heres what I think is the problem. I already had a T fitting on the vaccum line after the purge valve I was using for my boost gauge, so I used that for the MBC. Would this cause the CEL and the stalling? Im friggin freezing, so tomorrow Im going to move the T to before the purge valve and see if that makes a difference.
Thanks for any help.