ej22t SS, handicapped boost?
Posted: Fri Feb 11, 2011 7:41 am
My 92 legacy ss has a hallman MBC and forge BPV, wrx cold air setup (fender snorkel). Recently, i've noticed that the boost has gotten lower and lower on my Lamco gauge, when i got the car, the seller claimed he had it set of 13psi, but when i drove it, the gauge was only reading about 0.04 MPa, MAX. Which is something like 7psi?.. Anyhow, recently I've noticed it is only reading 0.03MPa, or about 5psi..
I wondered if my MBC was hooked up correctly, so i messed around, i found that the jam nut wasn't snug, so i naturally backed off the MBC all the way, ran the same boost, 0.03MPa.. Stop, crack jam nut loose, turn the MBC a bunch of turns in, started to feel some tension in the knob, figured that was the norm, so i tightened it back up and took it for a drive
I think i may have noticed a slightly more responsive boost, but again, 0.03MPa on the lamco gauge.
At this point i've stopped adjusting it, and i will probably investigate and insure that the factory solenoid isn't connected to anything and that the manifold-boost source is going into the bottom of my MBC and that the side nipple leads to my WG actuator.
I did however, notice that the compressor housing nipple had a hose on it still, so i will have to double check everything tomorrow..
I just don't want to find out that something is terminally wrong with my turbo, it's got 325,000 km on the car, doesn't make any bizzare noises, no screaming BOEING 747 noises from boost leaks under WOT, nuffin!
Also is it possible that my forge BPV is bleeding/recirc'ing boost and that is where it is being lost?
Thanks for the time guys.
I wondered if my MBC was hooked up correctly, so i messed around, i found that the jam nut wasn't snug, so i naturally backed off the MBC all the way, ran the same boost, 0.03MPa.. Stop, crack jam nut loose, turn the MBC a bunch of turns in, started to feel some tension in the knob, figured that was the norm, so i tightened it back up and took it for a drive
I think i may have noticed a slightly more responsive boost, but again, 0.03MPa on the lamco gauge.
At this point i've stopped adjusting it, and i will probably investigate and insure that the factory solenoid isn't connected to anything and that the manifold-boost source is going into the bottom of my MBC and that the side nipple leads to my WG actuator.
I did however, notice that the compressor housing nipple had a hose on it still, so i will have to double check everything tomorrow..
I just don't want to find out that something is terminally wrong with my turbo, it's got 325,000 km on the car, doesn't make any bizzare noises, no screaming BOEING 747 noises from boost leaks under WOT, nuffin!
Also is it possible that my forge BPV is bleeding/recirc'ing boost and that is where it is being lost?
Thanks for the time guys.