In the picture below, a couple things that I am not sure about to would be the crap quality hose clamps on the red hose. They are harbor freight clamps so maybe not a good seal would cause this issue?
Another thing, the hose from the IACV not having a clamp... would a small leak there cause this?

I had also shortened this hose about 8-10 in. I did not think that would cause any issues but that was another change. Or do I have something routed wrong here with the boost controller and the solenoid?

And here is a simple diagram of my catch can set up. had modified a previous one I saw on here. To me this setup is correct because everything gets routed back to the original spot.

Maybe I should have the boost control solenoid hose connect to the inlet at a different spot in comparison to IACV and purge valve?

That is everything I can think of. Any input is much appreciated, I would really like to get back to driving this car. I will be getting better clamps and double check the vacuum setup in the morning.