So, I swapped the #2 injector with the one in cylinder 4 thinking if it was the injector, the problem would move with the injector, it did not. There was some left over fuel in the rail when I swapped them over.
I tested the spark and plug outside the motor, looked good. I am using some msd universal wires I made. (yes I have the right leads on the coil going to the correct cylinders.)
Compression was 140.
No misfire codes.
Also, I am using the 22t engine harness for the 20g with a few slight modifications. Which was just extending the wires to the temp sensors.
Help
