High boost on stock controller.
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High boost on stock controller.
I recently changed over from my manual boost controller back to the stock system and found that I am sometimes spiking upwards of 15-16 lbs. It seems to run a consistent 10-12 lbs. at higher revs. I wanted to change back as I know the stock controller gives more consistent boost up to redline, but 15-16 is too high. Is there anything I can do? Oh I'm running a td-04. Thanks
94TW red.
What are you using to measure that boost level.
Josh
surrealmirage.com/subaru
1990 Legacy (AWD, 6MT, & EJ22T Swap)
2020 Outback Limted XT
If you need to get a hold of me please email me rather then pm
surrealmirage.com/subaru
1990 Legacy (AWD, 6MT, & EJ22T Swap)
2020 Outback Limted XT
If you need to get a hold of me please email me rather then pm
i'm using an autometer boost gauge, which i believe to be fairly accurate...maybe. i've only hit 15/16 once or twice before hearing some butt clenching tinging and letting off. i connected the wastegate directly to the compressor outlet and found that i would only get about 6 psi. with my manual boost controller set at 10 it also stays consistent. bad solenoid?
94TW red.
6psi on the stock TD04 wastegate actuator is low.. That's the VF11's.
I had an identical setup and ran an MBC and FCD. I ran 14 psi before the Revtronix chip install (now @ 17). Using my $15 NXS MBC I had consistent boost levels.
With the stock BCS I got boost creep up to 12-13 psi, which we attributed to (I think) my bellmouth downpipe/3" TBE.
Josh suggested I test my WG actuator w/a pump, and it was set to 10psi, which was the lowest I got running straight from the WG - 10 psi. This was w/the newer '06+ WG actuator. The older TD04's were higher.
From where RU reading boost?
I had an identical setup and ran an MBC and FCD. I ran 14 psi before the Revtronix chip install (now @ 17). Using my $15 NXS MBC I had consistent boost levels.
With the stock BCS I got boost creep up to 12-13 psi, which we attributed to (I think) my bellmouth downpipe/3" TBE.
Josh suggested I test my WG actuator w/a pump, and it was set to 10psi, which was the lowest I got running straight from the WG - 10 psi. This was w/the newer '06+ WG actuator. The older TD04's were higher.
From where RU reading boost?
Turbo Subies:
'87 GL-10 Turbo - SOLD
'90 BJ EJ22T/DOHC & 5speed swap - SOLD
'04 FXT, Forged internals, VF39, STI TMIC, Cobb AP- SOLD
'93 Legacy SS - 5-speed, SOLD :-(
'02 WRX -SOLD
'96 BD-turbo'd-SOLD
'98 SF - NA-T
'87 GL-10 Turbo - SOLD
'90 BJ EJ22T/DOHC & 5speed swap - SOLD
'04 FXT, Forged internals, VF39, STI TMIC, Cobb AP- SOLD
'93 Legacy SS - 5-speed, SOLD :-(
'02 WRX -SOLD
'96 BD-turbo'd-SOLD
'98 SF - NA-T